My 1993 R1 build thread! by fiz-e

By diyauto
( 1 )

7 minute(s) of a 75 minute read

6-13-2011

I was driving around with no passenger seat for a while and it did not really bother me! then one day I was driving my car and was stopped by a chick who needed directions... she literally cut her self off and said "wow, that's a really nice car, you need to give me a ride if your car" I told her I had no seat but yet she still got into the car in high heels and a cocktail dress and sat on the passenger floor where all my tools and stuff were laying! I gave her a ride, drove her back to where I picker her up from, got her number... and said! Damn I need to get a passenger seat! 


I picked up a set of Tan seats from a member (zeke542) who said he did not need them, super nice guy. I now was driving with a suede driver side seat and a Tan Leather passenger side seat! everyone who knows me from the meets knew how dumb that looked! but it was a seat! this was back in September of 09 wow I am way back on this stuff!


Shortly after I get the seats in and the clutch assembly together and am working on breaking in the car clutch. It was already getting close to winter and was time to put the car in the garage for the cold and then I decided to take the car out for one last spin around the neighborhood. I go to the gas station, and go over a small bridge from Brooklyn to LIC and gun it a little. Nothing was out of the ordinary while driving, car backfired as it did sometimes when I shifted harder. I come to a slow down at the light the car is barely staying on. I was like, WTF is this, did I run out of gas, or the alternator is dieing or something. 


I drive the car back to my garage while its smoking and backfiring like crazy... I am still talking to my self that its just a vacuum leak from the rats nest. that's all. that's all. and then Mobeoner comes by the garage and we test the compression just in case and the rear rotor reads a big fat 0. and that's how I ended the first season of my rotary owning experience. WITH A BLOWN MOTOR!



6-27-2011

After I blew that motor. the car sat there for a while and at one point my garage rent was increased way too high and the car needed to be moved to the new garage... luckily the car still started and ran on one rotor. me with mobeoner behind me drove to the new location which was about 6 miles away... car backfiring and smoking the whole way there. We get there and get all of our stuff moved in and after a little while of the car sitting there I went a little crazy with buying parts.


-I found a petit street ported motor with rebuilt turbos

-Power FC and commander

-Commander mount

-Greddy FMIC

-KOYO Radiator

-Greddy Pulleys

-Greddy Elbow

-new ignition coils

-Finally got matching base seats

and I am sure I am missing something but that was the jist of the purchasing.


and with that the swap was about to go underway.


Seats went out to make room for new seats.



After everything on the motor was back on... I ran into a small problem... the stock battery would not fit into the stock location because of the size of battery and the new koyo location. So not being able to wait... I went and got a small Optima battery which STILL did not fit in the stock location. so I ran some wires and had my battery located on my passenger side floor! (Many people joked about that for about 8 months that it stayed in that location)


With that we were able to turn the car over but could not warm it up for long because of the intense amount of smoke from the car... and the neighbors were bitching about the smoke... so we went and rolled out the car again to try to get it started and running outside in the lot,



After some issues with getting it started and then getting it to turn back on... (loose ground on the starter) the car was on and ready to smoke up the lot.







Car was not on and starting but had trouble starting back up while the car was hot. (I still have that problem) Car was also filthy as hell from being in a dusty garage for the winter.


oh yeah, and with the move from one garage to the other and after we had the motor in, we did not have enough room for all our stuff so we got a storage unit for the extra goodies that we did not need to use on a regular basis... 



soon after all that I took the car out for its inaugural ride and a much needed wash. ahhhh the car looked so good with the FMIC installed.




Car is on this set up untill this past friday, car runs better than before since we ripped out the rats nest and are now running non sequential twins... but with my luck there was a boost leak somewhere which till now I still can not find.


Car made it out to the carlisi meet



and to the five points meet



even made it to almost every thursday night meet and took it out as much as I could for the weekends.



Hell, even got myself a nice speeding ticket right before the winter... was clocked at 129 but the cop wrote it down to 109... still waiting on the court date to see what happens with this. (I did beat the new M3 though)



Since then for the winter the car has been sitting and I have been buying goodies for the car and getting ready for the single set up... the cars turbo was already blown from some thing... and the car just does not run right... so this will bring me to a quickened story of the rx7 life up until today. I am sure I missed some stuff but either way... I am excited on the changes happening now, and just wanted to get things caught up.




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