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9 minute(s) of a 15 minute read
5-16-2009
Turbo back from being rebuilt. Manifold and housing ceramic coated black. Microtech is here also.
6-6-2009
Its in.
6-21-2009
ll the drive train is finished up, hydraulics bled, and starter harness on so the car goes back to the ground. Getting closer.
7-15-2009
Update
8-22-2009
Microtech wiring finished, UIM back on, fuel finished, intercooler on, radiator on.
9-19-2009
Battery Box and battery are in.
9-24-2009
10-4-2009
Done.
12-13-2009
Still have to adjust the coilovers but you get the idea.
2-11-2010
part 2 of the project begins
3-20-2010
car made some progress today.
The old man working his magic....
3-27-2010
5-18-2010
minor progress
6-26-2010
7-5-2010
getting closer......
8-14-2010
crappy cell phone updates
8-24-2010
its finally home..
11-21-2010
Side skirts and wing are on..
1-22-2011
Update:
Now that the engine is broken in it is time to get some parts together so the car will be ready for tuning.
3-28-2011
New Turbo in..
4-24-2011
6-12-2011
12-17-2011
Installed Strut bar and B&M Line lock
11-10-2012
At it again. During mothers day weekend i turned on the car and heard a knocking noise. The higher the car revved the faster the knocking noise got. As i reached in to shut it off the motor took a dump. I covered the car back up and didn't mess with it for a month. I checked compression and it was telling me that the rear rotor had lost an apex seal. About a month after that i decided to pull the motor out and see what the damage was. As i pulled off the LIM a ceramic coating polishing ball dropped out of the LIM. I thought i had gotten them all out when i assembled it the first time but i guess not. ( My mistake ). When i disassembled the motor the only thing broken was an apex seal spring. I decided that since it was out and open again i was going to upgrade a few things. I decided to pin the motor this time around so i dropped off the motor at the machine shop for pining and the machinist dropped and broke my front plate. After spending almost a month searching for one i finally got the pining done. I also decided to go with the goopy seals instead of the Atkins seals that where in there already. I upgrade to a better quality turbo manifold and swapped out the HKS wastegate for a Tial.
1-6-2013
Motor back in..
2-10-2013
4-17-2015
After two years of only driving the car every now and then and not really touching it much.. I have gotten the itch to update some parts on it.
First was the wheels.. Decided to go with a Mesh style wheel... 18 x 9 / 10
a month ago i decided also to update the Rails and injectors going from the old KG / Stock set up to the FFE rails and newer version Bosch injectors.
During the summer when rain season starts the Microtech set up will be coming out and the Adaptronic will be going in..
Love all the pics!
Posted by Diggymart on 1/31/20 @ 7:31:09 PM